As mentioned earlier the Chernobyl reactor was a RBMK type of reactor which used graphite blocks surrounding the fuel channels as moderators. The water used as a coolant was driven by two electrically powered pumps from the bottom, this pressurised water flows through the channels absorbing heat from the reactor core and then the steam is separated which eventually is fed to a turbine to generate electricity (fig. 1 & 5).
The design of this reactor was such that it made possible for the reactor to sustain fission reaction with unenriched uranium without resorting to heavy water for moderation, which made it very cost-effective.
Now let's come to the happenings of that day.
That month in 1986 Chernobyl was schedule to shut down for refueling, which is done like once in a year to replace the used fuel with new fuel elements. And the operators wanted to Test a safety system during this power down phase of the reactor. Any nuclear reactor obviously requires some external electricity to operate. Mainly the coolant pumps need to be operated continuously because even after shutdown the core generates a lot of heat, termed as decay heat. Because the fuel is itself radioactive, they generate heat even when not undergoing fission. Usually power plants have diesel generators for backup power supply in an emergency. However, this generators would take a minute or so to come up to power. Hence, another power source was required for the first critical minute. As the first line of safety the backup power was supposed to come from power generated by the plant turbines itself. Even after shutdown the turbines would be spinning down under its own inertia-the flywheel effect and they wanted to test whether or not this power can be used to drive the coolant pumps for decay heat removal. This had never been demonstrated at Chernobyl. They wanted to turn off the reactor and they wanted to analyze the amount of steam that it would be producing which could be used for safe operation of the plant in case diesel generators fail.
Xenon Poisoning
Neutron absorption is critical in reactivity control in any nuclear reactor. Control rods are made up of suitable materials so that they can absorb neutrons properly. One of the fission products that builds up in the core is Xenon-135, which is exceptionally good at absorbing neutrons. Xenon does not appears instantly, about 95% comes from iodine-135 (half-life of 6.5 hours). The amount of Xenon grows until it reaches an equilibrium. When amount of Xenon increases, absorption of neutrons by Xenon means less absorption needed from the control rods. Xenon-135 is referred to as a “Neutron poison” in terms of nuclear engineering.
As it is evident that Xenon will form under normal operation, the operators adjust the control rod in such a way to keep the reactor at a constant rate. Xenon is actually burned by getting converted into Xenon-136 after absorbing a neutron (Fig. 8) during active conditions, which is stable and not a good neutron absorber. And if the reactor is not operating it will just decay into ceasium-135.
It is important to notice that at very low power levels the formation of Xenon-135 will continue at the rate of six and half an hour ago, but the burn rate is reduced now.
Hence, at such states the Xenon poisoning continues and it gets build up in the core slowing down the reaction.
The reactor was designed to operate at about
3200 MWth and their plan was to get the power output down to
700 MWth for conducting the simulation, while for the preceding few days before the accident the reactor was operating at
1600MWth.
The reduction of power began at around 11:10 PM from 1600MWth to 700 MWth. But in this process they inserted more control rods than required bringing down the power levels to 30 MWth instead of 700 MWth which was too low to run the test. At that point it was really difficult to bring up the power levels. [ MWth - Megawatts of thermal energy ]
The Xenon-135 was building up as there were no sufficient amount of neutrons being produced at low power levels to burn it up. But this was not the only effect that was eating away the neutrons in the core. Under normal operation water is boiled inside the reactor and boiling results in low density voids. This reduces the density effect and therefore neutron absorption. But during the low heat generation the water was not being boiled which means it was absorbing more neutrons than normal because water is a more effective absorber than steam.
However that day the power demands were higher than other days, that means reactor no.4 was not supposed run at such low power levels. Instead the reactor operated at a relatively higher power levels late into the evening.
In order to raise the power to such a level where they can conduct the test, the operators pulled a lot of control rods out of the reactor. For more effectiveness the design was made such that when the control rods were pulled out the process simultaneously pulled in graphite rods, or else the space would have been filled with water which is also a neutron absorber. And this process enhanced the reactivity as graphite acts a moderator. Normally there were 150-200 rods used in the reactor but as the Xenon was stealing all the neutrons coming under pressure they pulled out almost all control rods leaving behind only 7 to 8.
By doing this they were able to bring up the power to 200 MWth. This was well below the test protocol limits but high enough for generating steam to spin the turbines upto the operating speed. And hence the test began turbines were isolated and they began to spin down.
At this stage the things went wrong, at low power levels and and low coolant flow rate water has become a significant contributor of neutron absorption. The reactor became very sensitive to the boiling of water, as the water boils fewer neutron gets absorbed and they were moderated by the graphite rods sitting there in the core. This led to increase in the reactivity and in turn water boils more and more.
This positive feedback mechanism is described by the positive void coefficient. In a nutshell, it means that if the power (temperature) of the reactor goes up the reactivity tends to increase. As the power goes up the positive reactivity goes up, such designs of nuclear reactor is autocatalytic. Water is both a more efficient coolant and a more effective neutron absorber than steam, a change in the proportion of steam bubbles, or 'voids', in the coolant will result in a change in core reactivity. The ratio of these changes is termed the void coefficient of reactivity. When the void coefficient is negative, an increase in steam will lead to a decrease in reactivity. This is what makes the light water reactors safer.
The void co-efficient is one of the many such co-efficient that describes the reactivity under different conditions. And all reactors are designed in such a way that all these effects together result in a self-stabilizing reaction.
With the reactor in a low power and low flow state small changes in pressure, flow or temperature resulted in a power feedback loop and the power started to rise rapidly. So the water began to boil more in the lower sections of the reactor. At higher flow state the water pressure would push the voids up and the reactor would self-stabilize. As the operations were at low power and flow levels the reactor de-stabilized.
The only way before the operators was to quench the power to zero, for that they had to insert all the control rods at a time. But, unfortunately this was not a very fast process because the rods had to push down water in the channels out of their way.
Fig. 9:- RBMK-Core of Chernobyl-4: Positions of control rods (insertion depth in centimeters) approximately 1min30s before the explosion on Saturday, 26. April 1986, last signal of SKALA control system at 1:22:30 h.
If we consider the reactor geometry, the rods moved at about 40 centimeters per second and the core was about 7 meters long. So, it would take about 18 seconds to fully insert the rods. The control rods were also supposed to push down the reaction enhancing graphite rods, which were about 4.5 meters long. This means there was about 1.25 meters of gap at the bottom and at the top, this ensures that graphite rods are placed centrally for better reactivity control. Initially when the graphite rods were pushed down they replaced the water at the bottom. This rapidly enhanced the reactions at the bottom of the core as soon as they were trying to shut the reactor down.
What actually happened is in order to conduct the test the operators put the reactor into such a condition where they started getting the power but it became highly unstable. The process of shutting it down actually temporarily enhanced the reactivity for few moments and in these few seconds the power skyrocketed and went beyond design limits. Followed by this there were two subsequent explosions occurred, the second one a larger explosion blew off the roof of the building. The final power readings were found to be about 33 gigawatts but further studies suggest that the peak may have been reached as high as 300 gigawatts.
Some investigations shows that the second larger explosion may have been due to hydrogen explosion, at the power levels mentioned the water would have dissociated into hydrogen and oxygen by the heat and subsequently collecting and combusting.
Well I hope you got a good understanding on why and how the Nuclear reactor caused a mishap. We learn from mistakes and the present reactors are thus made as automatic as possible with enhanced control systems. The modern reactors are also well contained and designed with passive safety systems, which do not require any human intervention. The passive systems entirely depend on natural forces of convection and gravitation. In present generation reactors an explosion would be controlled more efficiently. For more information you may try these :-
0 Comments